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1. oan Lh N506RJ before its first flight on January 3 2006 Each of the taxi tests at progressively higher speeds gave me confidence in the plane engine and propeller It became a series of test a little fix a little test a little fix a little and repeat the process until everything was look ing good FIRST FLIGHT On January 3 2006 did a series of final taxi tests on a remedy to a nose wheel shimmy Every thing was fine at taxi speeds in 5 MPH increments from 50 to 80 MPH At 80 MPH gave slight aft pressure on the stick and the plane leapt off the runway and was almost instantane ously doing 100 and climbing rapidly With a big smile on my face immediately turned crosswind then downwind and had to pull the throttle back a bit since the plane was now doing 120 After stabilizing the speed at 100 pro ceeded to turn base then final and touched down at 100 mph The plane flew and landed beautifully with no shimmy or vibration so concluded that my vibration repairs were successful and coincidentally the first flight was magnificent was very pleased with the plane s per formance at partial throttle spent the next couple of days reinspecting everything retorquing the prop and getting ready for my second flight did a couple of full throttle ground run ups to check out the engine These were all rather short dura tion and no problems were indicated My flight plan for the next test flight was to do a
2. 4 250 or about 8 500 rpm to place it into limp home mode To get the tach pulse the engine team spliced a wire from the ECU to the igniter This pulse is 1 2 the engine rpm and closely approxi mates the prop rpm though the gear ratio for the prop is 1 1 8 not 1 2 so mentally add 200 rpm to the new tach reading to closely figure the actual prop rpm have not had another problem since and have been flying my airplane including full throttle for 5 years 195 hours since that most interesting day do use about 80 power for cruise and have the utmost confidence in the engine CASE STUDY ONE CONCLUSIONS One comment would like to make is that do not like the idea of trying to modify the ECU other than using the frequency divider as indicated above as ECU s are very complicated devices with so many parameters that messing around with the electronics is taking the chance of messing up something else The cure is really very simple use a simple digital frequency divider that is eas ily purchased at almost any electronic parts supply house One more thing as auto engines with a PSRU installed will usually run sans propeller because they are fitted with a flywheel test an auto engine before flying by re moving the propeller and run up the engine to a little above 4 600 rpm for about 2 minutes If the engine goes into limp home mode you have a problem that will need to be addressed As have mentioned abov
3. In a recent email to Larry and George reported that with the engine set up to Subaru specs have limp home mode indicated at low revs and can throttle up and go though the limp mode to the mid throttle range say bout 2k ish to about 3 750 or so RPM where limp mode is not present and normal running returns But then Limp mode returns again just prior to 4k rpm So with throttle movement in my installation can throttle back and forth through limp home mode From what understand from their experiences once they have en countered limp mode the engine was stuck in that mode That is not the case with my engine but keep in mind that my runs are only static i e aircraft chocked and stationary on the ground have a ground adjustable 3 blade propeller that has lots of pitch don t know the exact amount Full throttle run up only gets to a tad under 4k RPM when limp home mode kicks in However while in this mode at this throt tle position the engine revs come back to about 3 500 RPM so maybe only one injector is being shut down Two injectors are definitely shut down with the low throt tle position limp mode This testing experience adds even more reason for each owner builder to know his ECU and its behavior under various operating conditions Graham Brighton ig cmap and RECOMMENDATIONS If you convert an automobile engine to power an air craft or if you are already using such a conversion learn about the ECU and k
4. fuel filter or at least it was somehow related to the fuel system had n t heard of a limp home mode but soon got educated as to what actually happened that fateful day The limp home mode occurred at about 4 250 engine rpm in my Subaru Legacy engine and the reason my buns had been spared is the fact that had installed a 68 x 76 prop over pitched for that power of engine which never al lowed the engine to crank up to more than 4 200 rpm on takeoff Lucky me have since replaced the propeller with a 68x72 although that too is a little over pitched though am doing quite well with the newer prop then got in touch with the engine mod factory and indicated my displeasure and that expected immediate help to fix this thing A factory team of two flew into Detroit Metro rented a car and drove to Mason Airport and met them at Mason Jewett Airport in front of my hangar at the ap pointed time A Subaru portable engine analyzer was used to read the codes then it was determined that the engine power fail ure was indeed the so called limp home mode THE SOLUTION The cure was to use the wire from the ECU which nor mally is connected to a tachometer on the instrument panel and divert this to a digital frequency divider Thus whatever the tach signal read the divider returned the now divided signal to the ECU as half of the engine RPM The engine would never be able to generate a high enough signal double
5. glide o0 k but what speed had not yet established the best glide speed with this being only my third flight in this airplane VVM MMMUMMBMAVPRP PISS PYM E CONTACT issue ss pace 3 scanned the fields below me For the past two weeks it had been raining heavily and the ground was saturated with water saw a corn field to my right but rejected it as a poor choice kept gliding toward Mason Jewett Airport then finally saw the trap shooters field dead ahead still had enough altitude so mentally planned my approach Using my flaps as a control for descent first clicked in one notch maintaining 90 mph was still a little high but saw a ditch on the west end of the field and knew had to get over that pulled full flaps but then went back to one notch only to immediately go back to full and concentrate on my final approach The landing was perhaps the most beautiful landing have ever made and touched gently onto the sod Heaving a sigh of relief relaxed but should have imme diately applied brakes and shut down the engine As rolled out with the engine still idling and slowing down somewhat suddenly a slight depression with an elevated roadway appeared right in front of me and so while ap plying brakes and saying something like oh my good ness gracious in reality really said amp The pro peller dug into the soft ground throwing clay pigeons and dirt over the left wing and the a
6. noticing the problem advised the tower that had lost power did a quick visual check of the field to the left and it was full of field workers checked the freeway to the right and it was full of cars looked straight down and concluded was not high enough to go around So he 1 i E adta IEPA eemantenrnenane io sion masta Oc ire Limp home mode started here there was too high to get back to the runway and too low to go around What a way to start the morning The center of the field in front of me was still frozen in the middle of my windscreen so concluded was on a tra jectory to that spot in the middle of the field About that time the tower requested my intentions and muttered something about having to put the plane down Things were running through my mind pretty fast and this was about the time that recalled what had come up in a han gar discussion the week before One of the fellows men tioned that the famous pilot and air show performer Bob Hoover has once said something to the effect that if you are going to crash fly as far into the crash as you can and as slow as you can With this thought in the back of my mind continued evaluating the situation Here are a couple of complicating factors that raced through my mind e All the things could use in making the landing such as flaps slow flight characteristics and stall speed had not been determined or tested Not a cheery thoug
7. owners builders and pilots will not suffer our same experience CASE STUDY ONE By George Moore N6382G Jackson MI geomoor comcast net FIRST FLIGHT In October 2001 was finally ready for the first flight or perhaps should say first fright of my just completed KIS TR 1 powered by a Subaru Legacy 2 2 liter engine On the ground was Terry Lutz Terry is the first American test pilot to land the Airbus A380 on its maiden flight from London to Kennedy Airport Terry monitored the flight from the ground with a handheld radio while Tim Martinson flew chase in his beautiful RV 6A Terry had taken me up in his Luscombe a few days earlier to show me all the possible emergency landing fields around the airport one of which was the trap shooters field about two miles southwest of the airport was mentally pre pared and ready to go so lined up at the end of runway one zero at Mason Jewett Airport and with a dry mouth and a somewhat increased heart rate pressed the throt tle forward to full throttle The airplane picked up speed quickly and with one notch of flaps the airplane rose into the air flew south but stayed within about five miles of the airport and kept the speed of the airplane no more than 130 miles per hour as did not want to press my luck Everything went very smoothly except the left wing was somewhat heavy and could not communicate with Terry Lutz on the ground After trying some gentle turns and talkin
8. Why you Should Know your ECU Three Case Studies Reprinted by permission from the pages of CONTACT Magazine PO Box 1382 Hanford CA 93232 1382 United States of America 559 584 3306 559 585 0930 fax This article came attached with the following note from Larry David the person responsible for compil ing and submitting this article Pat The article that George Moore in Michigan Graham Brighton in Australia and in California collaborated on is attached In addition to all three of us owning Subaru Legacy 2 2L engine powered KIS TR1 aircraft and having experiences with the OEM ECU to share we did it all over the internet without ever having met each other in person While the technology of the ECU and its mysteries caused us some grief the technology of the internet helped us pull together this article and better understand the problems associated with the ECU INTRODUCTION This article contains three case studies from current owners of Subaru engine conversions These studies are provided in chronological order George Moore s ECU experience was in 2001 while Larry David s experience was in 2006 If similar cases had been publicized earlier both George and Larry might not have had such exciting experiences Graham Brighton has provided the results of his ECU testing which he started when he heard about the prior ECU issues reported in the first two cases We provide this information in the hope that other
9. against such a failure or sensors as may disable the drive the fail safe function is provided to ensure the minimal driv ability which is as close to limp home as could find Then on p 25 in the second footnote on that page the manual states When the engine operates at a speed greater then 2 000 RPM for more then 40 seconds a trouble code is emitted could find no statement as to what will happen after a trouble code is emitted How ever on p 26 in Table 5 TROUBLE CODES AND FAIL SAFE OPERATION there are descriptions of 23 trouble codes Ten of those codes have a Fail Safe operation described Two of those descriptions while not very clear in what they say do appear to be worrisome Code 23 Air flow sensor s fail safe operation is Controls the amount of fuel injected in relation to engine speed and throttle sensor position Code 24 Air control valve s fail safe operation is Prevents abnormal engine speed using fuel cut in relation to engine speed vehicle speed and throttle sensor position Trying to assimilate and inte grate these facts think it says when the engine runs for 40 seconds at greater then 2 000 RPM the ICU will start doing things and a couple of them involve reducing the fuel That s as close as could come to finding anything about limp home in the Subaru documentation Igdavid Larry David roadrunner com WG UUW 0000 002020 020 099 O O CONTACT issue 88
10. d the field straight ahead was still in the middle of the windscreen and looking better and better e The commercial growers use a planting bed tech nique where the field length growing beds are about four or so feet wide with a trench about a foot wide and a foot deep separating each bed The trenches are used for the farm machinery to drive in for wa tering the fields and for field workers to stand in when working the growing beds was approaching this field perpendicular to the trenches and growing beds and not inclined to try any sort of turns The good news is the fields had recently been picked so would not be damaging any crops and the fields were relatively soft figured when touched down it would be rough crossing the beds and dusty which it was Having considered all the possibilities could think of concentrated on my approach It appeared that my slightly controlled trajectory would clear the flood control ditch and the perimeter fence The middle of the field was still frozen in the middle of my windscreen and had become a welcome sight to me was able to maintain a tail low attitude The plane behaved great on the ap proach and thus far was uneventful Now the landing was something else As soon as the tail touched down grabbed the stick with both hands and pulled back with all my might closed my eyes gritted my teeth and held on because from that point on it was a sled ride There were scraping grindi
11. e the simplest way to solve this issue is to add is to add an inexpensive device a digital frequency divider hope this helps someone out there avoid the very seri ous problem of power failure when using an automobile engine conversion which has this feature built into the ECU George Moore CONTACT issue ss pace 4 CASE STUDY TWO By Larry David N506RJ Thousand Oaks CA INTRODUCTION My case began with an ad for a plane for sale on eBay The plane was a KIS TR 1 two place low winged fiberglass airplane powered by a 2 2 Su baru automobile conversion dilly dallied and did not get around to bidding while the plane was listed Later tracked down the seller and made him an offer and became the proud owner of N506RJ The plane was signed off for flight by the original builder but had been stored outside in the Phoenix sun for a couple of years after the original builder had decided with the help of his wife to donate the plane to a charitable organization The KIS kit was manufactured by Tri R Technologies in Oxnard CA The initial builder of N506RJ was a semi retired dentist in the Phoenix area and this was his fourth successful homebuilt aircraft project The engine was from a 1991 Subaru Legacy and was coupled with a Ross Engineering reduction drive The propeller was an in flight adjustable IVO Magnum The engine had the original equipment manufacturer OEM Electronic Con trol Unit ECU The ECU
12. e airspeed indicator which read 60 now instead of the 90 MPH it had indicated brief seconds before and the altimeter indicated 450 feet and was unwinding The ta chometer was indicating about 2 000 RPM the prop was still spinning at about 1 100 RPM and was moving but slower and not climbing This was not exactly what had planned for THIS CAN T BE GOOD When noticed the check engine light had come on was convinced that was experiencing a limp home situation like that experienced by George Moore another KIS owner in Michigan and described in case study 1 of this article After the off field landing people asked me if the first thing thought was Oh sh but strangely enough that thought never occurred Instead my emer gency training kicked in and busied myself with emer gency procedures jacked the throttle in and out to no avail Recalling that turning off the ignition switch was supposed to reset the ECU tried that twice also to no avail checked the fuel pressure and the fuel pumps they were all fine and the engine was running As was doing this was looking out and there was an empty commercial growing field straight ahead the center of which was smack dab in the middle of my windscreen As looked down at the runway and concluded was too high to get down to the little bit of runway available below and ahead of me About that point in time probably five or ten seconds after
13. full throttle run up full throttle taxi and take off at 90 MPH climb out at 90 level at about 4 500 over the field There would do some stall testing to determine actual stall speed slow flight testing to determine slow flight characteristics and flap testing to determine flight characteristics with flaps de ployed at 1 2 and 3 notches at various speeds THE EVENTFUL DAY On January 10 2006 verified that had 4 gallons of fuel in each tank taxied out to the run up area and did a full throttle preflight Everything was fine Then taxied out to runway two six commenting to the tower that while they were reporting a slight tail wind the birds sit JVV9 UG OUVX d 00000202020 07 Mu CONTACT issue s8 pace 5 ting on the wind sock indicated no wind When cleared for take off gave the plane full throttle accelerated to 90 MPH in about 15 seconds estimated rotated and began climbing at 90 MPH Between enjoying the view and the ride was checking speed al timeter engine rpm stick forces looking for any vibrations and mentally running my check list The field was quickly dropping away beneath me Then became aware minn sensed as it were that something had changed There was no pop bang thud vibration or anything to indicate a problem The prop noise level and exhaust noise level did not change The engine was running smoothly just sensed that was going slower which confirmed with th
14. g only to Tim Martinson because he was close by and could weakly pick up my radio transmissions decided to let Tim know that was going to return to the airport and do a landing The landing was great and even impressed Terry Lutz who was standing near the edge of the runway and as rolled past him Terry gave me a thumbs up taxied back to the hangar and the three of us danced around like idiots indicating unspeak able joy A few days later did a second cautious flight and once again all went well as my confidence was now building On the third flight a few days later de cided to fly west from Mason Jewett Airport and check out my radio to ascer tain what may be the difficulty As it turned out it was a defective device that had installed on my instrument panel that was supposed to allow me to use a hand held radio as a backup connected to the aircrafts antenna Not being able to reach Lansing approach decided to increase my altitude from 3 500 ft to 4 500 as was flying west again tried the radio no response from Lansing so decided to push the throttle to near full and see just how fast this little bird could split the air After about a minute with an rpm of 4 300 suddenly and without warning the engine shut down with a slight cough but continued to idle never felt so alone in my life Immediately while turning back 180 toward Mason Jewett Airport went through the emergency procedures and set up a
15. ht e Several of the KIS TR1s had demonstrated a ten dency to drop the nose at slow landing speeds in ground effect resulting in bent nose gears and prop strikes Not wanting to lower the nose to increase my speed for fear of overshooting my landing spot and going into the hot house structures in the next field figured had better land tail low the best chance of not snapping the nose down and flipping over e A short distance beyond the end of the runway was a flood control ditch full of rip rap large boulders that ran perpendicular to the runway Obviously my survival depended on clearing that ditch so whatever did had to clear that obstacle e A short distance beyond that flood control ditch was the airport property security fence which is about 6 feet tall This obstacle while worrisome was proba bly not lethal if plowed into it e R R RR RRR CONTA CT ISSUE 88 PAGE 6 N506RJ after its second flight at rest in the celery field adjacent to the airport e The actual stall speed of this plane had not been determined Some of these planes had been re ported as stalling as fast as 70 MPH a rather worri some thought The advertised stall speed was 58 MPH and fortunately for me because the plane was so slick was doing 60 and had not stalled yet had a 2 MPH margin of error before might stall an other worrisome thought With only a small margin for error stall opted to not try to make any turns an
16. irplane stopped abruptly Three men walking a dog in the area observed my ap proach and touchdown One of the men lived at the site and offered me his pole barn where he said could effect repairs This was a very kind gesture but declined stat ing that had to secure the services of a flatbed truck and get the aircraft back to the airport only about 2 miles away The other man who had a pickup truck and dog offered me a ride back to the airport an offer accepted Jack Tomen watched me leave via airplane and was as tonished to see me get out of a pickup truck right in front of his hangar where he was working on his project a Kitfox Jack s mouth dropped open and said George where is your airplane wanted to tell him that was a magician and that made my airplane disappear but instead explained what happened thanked the kind gentleman who had returned me to the airport and Jack dropped everything and agreed to use his SUV to chauf feur me to a towing service nearby The rest is rather uneventful only to say that we had a convoy of two police cars ahead followed by a tilt bed truck with the airplane sitting proudly or ashamedly on that truck bed with Jack and me following right behind We drove through a resi dential area where gawking children stopped their play to look in wonder at this white airplane on a truck bed as we slowly moved past PROBLEM ANALYSIS At first mistakenly thought it was a blocked
17. ng and tearing sounds as was bounced around a lot When the dust settled opened my eyes and the remainder of the cel ery crop was just beyond my feet The nose of the plane had taken a left turn probably because the engine was still running and the prop was still turning at about 1 100 RPM estimate that decelerated from 88 FPS 60 MPH forward speed and about 8 10 feet per second descending to zero in about 30 40 feet My tail low strat egy worked in the soft field The plane had not flipped over The main gear was located about 30 feet behind the final resting place The folks who removed the plane from the field said the nose wheel had nicely folded back under the plane and gouged a ditch about a foot deep and about 6 8 feet long that was visible when they lifted the plane onto the truck Based on the adage that any landing you can walk away from is a good landing and if you can use the plane again it is a great landing This would qualify as a good landing walked away from the landing with a little help from the rescue helicopter folks also got a free helicop ter ride and got to know a lot of really nice people at St John s Medical Center in Oxnard WHAT HAPPENED or POST CRASH ANALYSIS All indications are that the OEM ECU sensed some con dition that it was programmed to believe was catastro phic for the engine and shut it down to limp home mode In an automobile this is a very handy feature since it allow
18. now exactly what the ECU is going to do under all operating conditions In Larry s case maximum power for about a minute resulted in a broken plane Thorough testing like Graham is doing would have prevented this out come Modifying the tach signal such as George has done would also have prevented the problem 2 When flight testing get as high as possible as soon as possible In Larry s case he used too much of the 6 010 foot runway with the 90 MPH speed 90 MPH covers 132 fps or 7 920 feet per minute Calcula tions by the late Vance Jaqua indicated at that 90 MPH in the KIS it should have been climbing at over 1 500 feet per minute but in fact after about a min ute the plane was only at 450 feet This suggests the limp home mode occurred in less then a minute Testing like Graham is doing would confirm the exact behavior of the ECU 3 Always plan for and anticipate that the engine could quit or lose power on take off Larry is often heard muttering over 30 years of flying without an incident and then this So it can happen and like Murphy s Law it will happen at the worst possible time Footnotes The 1991 Subaru Legacy Service Manual never clearly describes the limp home mode On p 24 section 6 in the self diagnosis system describes that the self diagnosis system detects and indicates a fault in various inputs and outputs and turns on a warning lamp Check Engine to indicate a fault has occurred Further
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20. receives signals sent from various sensors and switches to judge the engine operat ing condition and emits output signals to provide the opti mum control and or functioning of various sys tems Source page 13 Subaru Legacy 1991 Service Manual section 2 This was a 90 completed project You have heard of the 90 10 rule It takes 10 percent of the time to get a project 90 completed and 90 of the time to do the last 10 While had joked about that rule for many years as a systems engineer experienced it first hand as an aircraft builder during the four years completed the construction of the plane One of the most challenging and most rewarding parts of building or finishing in my case an experimental aircraft is the testing process After reassembling the aircraft from its trip by trailer from Mesa AZ to Camarillo CA started the process of finishing and testing it There were a number of major things that resulted from the two years of neglect while the plane sat out in the Phoenix sun A cracked windscreen needed to be replaced major fuel tank leaks had to be repaired and the weak nose gear was replaced along with numerous cosmetic de tails As things were fixed the testing began in earnest with a series of ground run ups that identified expected things like fuel oil and water leaks which were not sur prising and were all easily remedied Taxi testing found various vibrations and shimmies that were also fixed
21. s you to limp home at 20 25 MPH so you can get it fixed but not so good for an airplane It appeared that when the engine was run at full throttle for some predetermined length of time in my case it ap peared to be about a minute at about 4 600 RPM the ECU reduced the power down to about 2 200 Probably the reason it didn t happen during the first flight was was only using partial throttle The previous occurrence of limp home in Michigan happened at altitude after the pilot completed his climb and started a high speed test run see case study 1 for details Larry David YJds5 BOO PQOPP LMM CONTA CT ISSUE 88 PAGE 7 Case Number Three By Graham Brighton N202DR Victoria Australia gbrighton net tech com au Based on George s and Larry s experiences in case studies one and two was a bit apprehensive about my recent purchase of a Subaru powered KIS had already exported it from the USA to Australia so had to find out what the situation was before bent my new plane The laws here require use the talents of local mechanics do all my work so enlisted the services of several different experts claiming Subaru ECU experience in order to better understand the ECU behavior with the hopes of avoiding the same experiences as George and Larry Our testing has determined that somewhere above 4 000 RPM the ECU turns off one or two of the four injectors leaving the engine running on in limp home mode

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